Monday, December 10, 2012

Kimball J-93 Hydrostatic Conversion


The J-93 was another project that originated with my father-in-lawAs the story goes, the J-93 was discovered at a neighbor's house while my FIL was helping my brother-in-law.  This poor thing apparently had a rough life and was missing the majority of its drivetrain.  The neighbor's son had made an effort in install an old Honda ATV engine/transmission, but gave up and sold it to my FIL.


J-93s (4x2) and J-98s (4x4) were built by Kimball Products in Benton Harbor MI.  There is not a lot of information on the web regarding these UTVs, but they appear to be related to Heald Haulers and look like a mini-Jeep, so there is an instant cool factor.

J-93s originally came with a 16HP Briggs & Stratton engine driving a CVT that fed a 3-speed+Reverse transmission and a chain final drive.  This unit only had the chain drive and the axle remaining.  Here is how it showed up at my place:



Harbor Freight was clearancing out their Greyhound line of engines, which were produced by Lifan.  These are one of the better quality Honda clones as I found out later.  The engine for this project is a copy of a Honda GX340 with electric start and is rated for 11HP and 19.5 ft-lb of torque.

After looking at what I had to work with, I began formulating a plan.  Option 1 was to find a transmission and fab up a CVT drive and the other missing components.  Option 2 was an idea I came up with a couple of weeks after receiving the project.  Given how this UTV was going to be used, I decided to try something new and build a hydrostatic drive.  Surplus Center in Lincoln, NE is a great source for power transmission parts, so I began my search there.  Adapting a hydrostatic drive to the J-93 would require some addtional fabbing and calculations, so a lot of layout work would be necessary.  Snag #1: The engine and pump ended up being too long and would not package sideways, so I have to drop it in length-wise.


It wasn't long before I hit snag #2:  The engine output shaft was too long and the mounting holes for the pump adapter were double threaded and completely worthless.  Not insurmountable problems, but nuisances nonetheless.  Then came snag #3:  In my rush to get parts, I neglected to think through how I was going to mount the alternator for charging the battery and running the accessories.  Originally it was going to be driven off the output shaft like everything else, but with the new pump mount, that option was out the window.  Discouraged, I thought about it for a few days and came up with an idea.

Start with an aluminum timing pulley I had laying around:


Do a little CAD work on my lunch break:


And you end up with a cool pulley adapter for the flywheel side of the engine:






Getting the drive pulley mounted was a huge weight off my shoulders and I could get back to the regular work, including taking care of the Snag #2 issues and putting the engine and pump together along with mounting the alternator.

The solution to the screwed up mounting holes was to Helicoil them, which had the added benefit of placing steels threads where there had been aluminum threads.

 



With the engine/pump combo finished I turned attention to the rest of the system.  The motor was fairly easy to mount up, just needed to mount the sprockets square to each other.


Mounting the hydraulic reservoir required some forethought of hose routing and ultimately the mounting tabs had to be cut off and new ones welded on the top.  Every component needed to be flush or below the top of the frame to provide clearance for the dump bed.  Not obvious, but the filler neck was shorten until the cap sat flat on the top of the tank.
A strainer was used to keep major debris in the tank and protect the charge pump.
The minimum filtration requirement between the pump and motor was 25 micron, I was able to source a 20 micron filter and installed it in the return line.  The hydrostatic pump circulates the majority of the fluid between the pump and motor.  The charge pump keeps the primary loop "full", pushing in more fluid from the reservoir as fluid is lost to leakage and returned to the reservoir via the filter.

Here is the complete setup as I tested it.  It stills needs a control linkage and wiring, but my father-in-law is going to take the project from this point.

Loaded up and headed to it's new home.  It still needs new paint, a seat and a bumper.  I hope to update this post when it is completely done.

A short clip of the first test run:


Sunday, November 25, 2012

A Few Misc. Projects

Sometimes a custom solution is needed for a particular job, as was the case of our friends who needed a railing for their back door, but wanted something a little nicer
Prior to powdercoat


Other times a replacement part is hard to find, like old John Deere brackets



And still other times it's cheaper to build it yourself.  Here is a my first attempt at an edge lit sign

 
And a large version I built for my church


'57 Chevy Sign

This is an old project my father-in-law brought to me.  He wanted to build a new sign for my mother-in-law's business and had a '57 Chevy in very poor condition sitting in a back field.  I received the back half with generic instructions to modify it so it would bolt to the side of the a building.


The first step was to plan out a mounting scheme and determine how much the final weight of the sign should be, then cut it down appropriately.  I decided to only retain the trunk poriton of the car.  After scribing a parting line, I remove the inner portion of the car that was not needed, taking care to ensure it would mount flush to the building with no gaps or waviness.

The next step was to remove as much weight as possible without compromising the structure of the trunk area and add back in the necessary framework to mount it to the side of a building.  The threaded rods visible in the picture are vertical support legs I added for stability.  In the end the sign rigging crew commented that the internal framework was some of the better work they had seen and stated in their experience, the legs were unnecessary.

With the factory frame removed for weight savings, I had to fabricate mounts for the bumper, taking care to get it in its original position.  Additionally I removed the trunk lid hinges and latch and replaced them with 1/4" bolts to hold everything together. 

Here's the final product after a trip to the body shop and being mounted to the building.  My FIL spent a fair amount of time digging up new trim pieces and a bumper due to the originals being rotten paper thin in spots.
I was quite impressed with the work the body shop did, considering I swept up over 150 lbs of rust that fell off the car during the construction process. 

Sunday, October 28, 2012

Getting Started, The Auto Case Trimmer

For those of you that are precision shooters, you probably load your own cartridges and are aware of how time consuming case prep can be.  I purchased a RCBS Trim Pro Power Case Trimmer to help speed the process along.  Although it helped, it was still time consuming to load and unload the cases and did not leave my hands free for the deburring op.  One day I got to looking at my pile of parts and decided to add a few pneumatic cylinders, flow controls, and a foot valve to the trimmer.


The end result is crude, but my foot now controls the two levers that use to require my hands and has freed up enough time between cases that I can trim and debur simultaneously.  This video was shot with an old camera that wouldn't focus, but you get the idea: